Air Emission Event Report Database Incident 354646
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| Incident Tracking Number: |
354646 |
Incident Status: |
OPEN |
| Report Type: |
INITIAL |
Report Date: |
04/23/2021
|
| Name of Owner or Operator: |
TARGA MIDSTREAM SERVICES LLC
|
CN: |
CN601301559
|
| Regulated Entity Name: |
SAND HILLS GAS PLANT |
RN: |
RN102552031 |
| Physical Location: |
5601 FM 1053 |
| County: |
CRANE |
| Event/Activity Type: |
EMISSIONS EVENT
|
| Date and Time Event Discovered or Scheduled Activity Start: |
04/22/2021 09:00 AM
|
| Date and Time Event or Scheduled Activity Ended: |
04/22/2021 01:00 PM
|
| Event Duration: |
4 hours, 0 minutes
|
| Process Unit or Area Common Names |
| Sandhills Gas Plant |
| Facility Common Name |
Facility Identification Number (FIN) |
| Acid gas compressor |
C-14 |
| 1 - Emission Point Common Name: |
Emission Point Number: |
| Emergency acid gas flare |
F-4 |
| List of Air Contaminant Compounds - 2 total |
| Description |
Est. Quantity/ Opacity |
Units |
Emission Limit |
Units |
Authorization |
|
Hydrogen Sulfide
|
100.0
|
POUNDS
|
0.0
|
|
Permit #53135
|
|
Sulfur dioxide
|
20000.0
|
POUNDS
|
0.0
|
|
Permit # 53135
|
| Cause of Emission Event or Excess Opacity Event, or Reason for Scheduled Activity: |
| Acid gas compressor was shut down due to high 4th stage scrubber level. With unit down acid gas volumes blended with residue quality enrichment fuel were routed to the emergency flare F-4. |
| Actions Taken, or Being Taken, to Minimize Emissions And/or Correct the Situation: |
| Instrumentation and electrical technicians worked to correct electrical failure causing the high level. |
| Basis Used to Determine Quantities and Any Additional Information Necessary to Evaluate the Event: |
|
| Initial Notification Date/Time: |
04/23/2021 08:27 AM
|
Method: |
STEERS |
| Notification Jurisdictions: |
REGION 07 - MIDLAND
|
| Publication Status: |
VERIFIED BY A CUSTOMER |
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